Development of a Unique Process for Recovery of Uranium from

Oct 15, 2010 - Figure 1. Bench-Scale SC CO2 Setup for Uranium Extraction Tests. ... Increasing the temperature from 50°C to 70°C greatly increased t...
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Chapter 6

Development of a Unique Process for Recovery of Uranium from Incinerator Ash Sydney S. Koegler* AREVA NP Inc., 2101 Horn Rapids Road, Richland, WA 99354 *[email protected]

A unique new industrial process has been developed that recovers uranium from incinerator ash produced by nuclear fuel fabrication plants. The process utilizes nitric acid and tri-n-butylphosphate (TBP) dissolved in supercritical carbon dioxide to extract uranium oxide directly into the supercritical fluid without a separate acid dissolution step. The process was developed in phases beginning with bench-scale feasibility tests and concluding with pilot plant demonstration tests. The bench-scale feasibility experiments tested basic chemistry and the ability of the process to extract uranium from incinerator ash. Pilot-scale tests determined practical operating conditions and scale-up factors for the design and implementation of a full-scale process. AREVA NP Inc. completed construction of a full-scale ash uranium plant in 2009 that will allow safe and environmentally friendly uranium recovery from ash and other low-uranium materials that would otherwise be uneconomic if done by conventional methods.

Introduction In 2003 AREVA NP Inc. (then Framatome) in cooperation with the University of Idaho began developing a unique new process to recover uranium from incinerator ash. The program was driven by a need for a lower cost and more environmentally satisfactory way to recover uranium from the 30-plus metric tons of incinerator ash produced at the Richland nuclear fuel fabrication site during 20 years of burning uranium-contaminated combustible waste. © 2010 American Chemical Society In Nuclear Energy and the Environment; Wai, C., et al.; ACS Symposium Series; American Chemical Society: Washington, DC, 2010.

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Nuclear fuel fabrication combustible waste comprises paper wipes and rags, shoe covers, worn-out protective clothing, plastic, and other materials that have become contaminated with uranium during uranium fuel fabrication for the nuclear power industry. The high cost of direct disposal of combustible waste drove AREVA to install an incinerator in the early 1980’s to reduce the volume of waste with plans to eventually recover the enriched uranium contained in the ash. Incineration of the combustible waste reduces its mass by 20 to one, and hence its disposal cost is greatly reduced, but the ash still contains valuable enriched uranium. AREVA tested recovery of the uranium from incinerator ash using its nitric acid dissolution and solvent extraction processes, but found that these processes were costly and produced undesirable wastes, and therefore, a replacement technology was needed. Although a supercritical (SC) CO2 uranium recovery process held the promise of a more efficient, cleaner method, it required significant development work to implement a commercially viable process. This chapter describes the development process.

Process Description Carbon dioxide is an excellent solvent for certain organics under supercritical conditions, i.e. temperature greater than 31°C and pressure greater than 73 bar (1070 psi), and its solvent properties can be modified by adjusting temperature and pressure. The efficacy of the SC CO2 process for uranium recovery lies in the unique properties of the supercritical fluid. Because SC CO2 has gas-like properties (low viscosity and surface tension) it can flow easily through a bed of ash. Its liquid-like properties, relatively high-density and solvation properties, make it possible for it to extract metals directly into the SC fluid without a separate acid dissolution step. The AREVA SC CO2 uranium recovery process is based on technology developed jointly with University of Idaho (1). It recovers uranium from ash and other low-uranium content material using a tri-n-butylphosphate (TBP) and nitric acid complex, TBP(HNO3)x(H2O)y, dissolved in SC CO2. The SC CO2 process is an improvement upon the existing AREVA uranium recovery processes for low-uranium materials that use a nitric acid leach followed by TBP-dodecane solvent extraction. Although the existing process was demonstrated to be workable, the low-uranium-content uranyl nitrate solution produced by the traditional process makes uranium recovery via this route economically unattractive. The SC CO2 process is better than the traditional solvent extraction process because it recovers a larger fraction of the uranium, eliminates the separate nitric acid dissolution step, and is less costly to operate. Environmental performance is also improved with the SC CO2 process because it requires no NOx treatment and produces no off-gas treatment effluent, and it creates an easy-to-handle solid waste ash residue.

66 In Nuclear Energy and the Environment; Wai, C., et al.; ACS Symposium Series; American Chemical Society: Washington, DC, 2010.

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Feasibility Tests The development of the SC CO2 process began with feasibility testing. Dr. Chien Wai and his associates at the University of Idaho showed that uranium oxide can be dissolved in SC CO2 with the use of tributyl phosphate (TBP) as a cosolvent and nitric acid as an oxidizer (2–4). This chemistry is similar to that of the Plutonium Uranium Extraction (PUREX) process developed in the 1960s for recycle of spent nuclear fuel. Bench-scale feasibility tests carried out at AREVA demonstrated that the SC CO2 process could extract uranium directly from incinerator ash. The goals of the feasibility tests were to determine if uranium could be effectively extracted from incinerator ash and then separated from the other co-dissolved metals so that the uranium could be recycled in AREVA’s fuel fabrication process. Uranium Extraction Feasibility Test Results The experimental set-up for the uranium extraction tests is shown in Figure 1. For the extraction tests the nitric-acid-saturated TBP was placed in a cell and SC CO2, supplied by a high-pressure syringe pump, was pumped into the cell and carried the TBP into a extraction chamber containing the ash test sample. The ash, SC CO2, and TBP were held at temperature for a prescribed amount of time and then discharged to a lower-pressure separation chamber where the CO2 vaporized and the TBP separated from the CO2 gas. The TBP was then analyzed for uranium to determine extraction efficiency. The bench-scale tests demonstrated that the key parameters for uranium extraction are temperature, pressure, TBP concentration in the SC CO2, nitric acid content of the TBP, and extraction time. The temperature and pressure determine the density of the SC CO2 and the TBP solubility. A higher temperature also improves the reaction kinetics and hence the extraction rate. However, a higher temperature also decreases the SC CO2 density and with it the solubility of TBP. Higher nitric acid content increases the oxidation rate of UO2 to the uranyl ion (UO2+2). For these tests the TBP was saturated with the maximum nitric acid possible in a single-stage batch contact before its use in the SC CO2 test. An important result of the batch feasibility tests was that under the proper conditions more than 90 percent of the uranium could be extracted from incinerator ash in less than four hours. Chemical Separations Feasibility Test Results Another objective of the feasibility tests was to determine if once the uranium was extracted from the incinerator ash, it could be separated from the other co-extracted materials to purify it for recycle in the AREVA uranium fuel fabrication process. In the chemical separations tests TBP which had been loaded with uranium in the extraction tests was contacted with an aqueous phase containing various amounts of water and nitric acid. It was expected, based on extraction data from the PUREX process that a separation could be made between 67 In Nuclear Energy and the Environment; Wai, C., et al.; ACS Symposium Series; American Chemical Society: Washington, DC, 2010.

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Figure 1. Bench-Scale SC CO2 Setup for Uranium Extraction Tests. the uranium and metals, but the performance under supercritical conditions was unknown. The experimental setup for the separations tests was similar to the extraction test setup. The uranium-loaded TBP was placed in a cell through which SC CO2 was pumped to carry it into a reaction cell. The reaction cell contained the aqueous phase comprising various concentrations of nitric acid. The TBP-SC CO2 solution and aqueous phase solution were mixed for a specified time and then transferred through a pressure reduction valve to a low pressure vessel to separate the CO2 gas from the TBP and aqueous solutions. The TBP and aqueous samples were then analyzed for uranium, metals, and acid content. The distribution coefficients (metal concentration in TBP divided by concentration in aqueous) are shown for uranium and other co-extracted metals in Figures 2 and 3. The separations test data showed that the uranium distribution coefficient was much higher than the distribution coefficients of the other metals at high nitric acid concentrations. This implied that uranium could be partitioned from the other metals in a “scrub” step. In the scrub step, at a suitable nitric acid concentration, the contaminating metals will transfer to the nitric acid aqueous phase leaving the uranium behind in the TBP phase. The test data also showed that uranium has a low distribution coefficient at a low nitric acid concentration and therefore uranium could be removed from the TBP after its purification in a “strip” step using water or diluted acid.

Pilot Plant Tests The next phase in the development of the SC CO2 uranium recovery process was pilot plant testing. The pilot plant tests included one-pass experiments to test individual process steps, a series of continuous pilot-plant tests where the entire process was tested as a unit, and intermediate-scale column tests that used a larger separation column to determine scale-up parameters for the chemical separations (scrub and strip) steps. Extraction Test Apparatus The pilot plant extraction test apparatus comprised two, one-liter, stainless steel extraction vessels with removable baskets, and auxiliary equipment including pumps, heaters, and hold tanks. The extractor vessels used for the batch 68 In Nuclear Energy and the Environment; Wai, C., et al.; ACS Symposium Series; American Chemical Society: Washington, DC, 2010.

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Figure 2. Uranium Distribution Coefficient as a Function of Free HNO3 Concentration

Figure 3. Metals Distribution Coefficients as Functions of Free HNO3 Concentration extraction tests are shown in Figure 4. The extractor vessels, CO2 vaporization tank, CO2 pressure-let-down valves, and feed lines were heated with electric resistance heaters controlled by stand-alone controllers using surface-mounted thermocouples. Incinerator ash or other low-uranium feed material was placed in the extractor baskets and the TBP-HNO3-SC CO2 extractant solution was pumped through the static material in either down-flow or up-flow mode. When using the up-flow configuration, a sintered metal frit-and holder screwed into the lid kept the ash from being carried out with the SC CO2 extraction solution. 69 In Nuclear Energy and the Environment; Wai, C., et al.; ACS Symposium Series; American Chemical Society: Washington, DC, 2010.

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Figure 4. Pilot Plant Extraction Vessels Used for Uranium Recovery from Incinerator Ash Key Pilot Plant Extraction Test Results The pilot plant extraction tests confirmed that time, temperature, and nitric acid concentration are key parameters for uranium extraction from incinerator ash. The extraction tests also demonstrated that ash particle size is important and that uranium extracts differently from ash obtained by burning different types of combustible material. Uranium extracted from the ash initially at a relatively constant rate and gradually decreased with time as the uranium was depleted as shown in Figure 5. Extraction at 70°C for four-to-six hours removed more than 90 percent of the uranium from the ash. Increasing the temperature from 50°C to 70°C greatly increased the uranium extraction rate. However, TBP-dodecane solvent extraction experience has shown that temperatures above about 70°C can degrade TBP, producing dibutyl phosphate (DBP) and phosphoric acid. DBP tends to extract uranium, but does not allow the uranium to be stripped out with water under normal process conditions. Therefore, extraction temperatures above 70°C must be avoided. Figure 6 shows that uranium extraction efficiency increases as the nitric acid concentration in the TBP increases. Increasing the free TBP nitric acid content from 3.6 M to 6.0 M significantly improved the extraction rate. Effect of Other Parameters on Uranium Extraction Ash produced from different sources of combustible material extracted differently. Uranium extracted more easily from ash produced from a mix of combustible material containing mainly paper and wood as opposed to ash 70 In Nuclear Energy and the Environment; Wai, C., et al.; ACS Symposium Series; American Chemical Society: Washington, DC, 2010.

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Figure 5. Effect of Time and Temperature on Uranium Extraction

Figure 6. Effect of TBP Nitric Acid Concentration on Uranium Extraction produced from another mix of combustible material with a higher fraction of plastics. Although the two types of ash were produced in the same incinerator at approximately the same temperature and residence time, they varied in density, pH, and particle size. These parameters may have affected the ability of the TBP-HNO3-SC CO2 mixture to intimately contact and extract uranium form the ash particles. It is likely that incinerator ash or other uranium-containing material from any new source will require a test to determine extraction parameters before sending it to the full-scale plant. Chemical Separation Test Results The chemical separation tests demonstrated the steps necessary to purify the uranium extracted from the incinerator ash in a form suitable for recycle in the 71 In Nuclear Energy and the Environment; Wai, C., et al.; ACS Symposium Series; American Chemical Society: Washington, DC, 2010.

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AREVA fuel-fabrication process. The separations processes tested in the chemical separation experiments were uranium purification (scrubbing), uranium removal (stripping), and acidification of TBP. The separations tests used a packed column to provide contact for mass transfer between the SC CO2-TBP stream and an aqueous stream. Two different one-inch (0.025 m) inside-diameter (ID) packedbed columns were used in the tests. The smaller column had a packing height of 31 inches (0.8 m) and the taller column had a packed height of 81.5 inches (2.1 m). The taller column is shown in Figure 7. The columns were heated by wrapping them in electrical heat tape. Several packing materials were tested, including stainless steel mesh and stainless steel and ceramic rings. Water or nitric acid scrub/strip solution (aqueous phase) was pumped into the column near the top through a spray nozzle and droplets flowed downward, while a SC CO2-TBP solution (organic phase) was pumped into the column near the bottom and flowed upward. The heavier aqueous phase coalesced at the bottom of the column below the SC CO2-TBP inlet point and was removed from the column. The organic phase was discharged from the top of the column through a pressure-reduction valve into a phase-separation tank where the liquid TBP/ uranium solution separated from the vaporized CO2 and the CO2 was discharged to the vent system. Acidification of TBP A single batch contact between pure TBP and 70 percent (15.6 M) nitric acid produces a TBP-nitric acid solution containing about 3.6 M nitric acid. The TBP nitric acid content can be increased substantially by contacting the TBP with nitric acid in a counter-current column. A series of TBP acidification tests were conducted with the separations columns to test the counter-current acidification of TBP. The nitric acid concentration in the organic (TBP-CO2) and aqueous phases exiting the columns was determined by titrating the solutions with sodium hydroxide. The tests showed that TBP-nitric solution acid concentration was directly proportional to the aqueous nitric acid concentration injected at the top of the column. There was also a small effect of the aqueous-to-organic flow ratio. There was little difference in organic solution nitric acid concentration between tests run at different flow rates, or between tests run on the 0.8m and 2.1m columns. Nitric Acid Scrub Test Results Several “scrubbing” tests were conducted in which the TBP/HNO3/uranium solution (organic) from the extraction tests was re-dissolved in SC CO2 and pumped upward through the packed column while a nitric acid scrub solution was pumped downward through the column. The purpose of the scrub step is to cause the contaminating materials that were co-extracted with the uranium to be transferred into the nitric acid scrub stream while the uranium remains in the TBP-SC CO2 stream. The scrub column experiments tested the effects of scrubbing parameters including stream flow rate and nitric acid concentration on contaminate removal from the uranium-TBP stream and uranium loss to 72 In Nuclear Energy and the Environment; Wai, C., et al.; ACS Symposium Series; American Chemical Society: Washington, DC, 2010.

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the aqueous-scrub stream. Concentrations of uranium and contaminants were measured in both the aqueous and organic phases at the conclusion of each test. The scrubbing experiments tested varying aqueous and organic flows with nitric acid at concentrations between 0.5 and 10 molar sprayed into the top of the column. The effect of column height was also tested. Scrub solution nitric acid concentration and flow rate affected both the contaminant removal efficiency and uranium loss (uranium scrubbed out with contaminants). Higher scrub feed nitric acid concentration and flow improved the removal of contaminants from the organic (TBP-SC CO2) stream. Uranium lost to the aqueous scrub increased with the scrub flow rate and was higher in the taller column than the shorter column. An important implication of these results is that there is an inherent trade off between uranium purification and uranium loss to the aqueous effluent. The same parameters that improve uranium purity (high flow, high acid concentration) also cause more uranium to be lost to the aqueous effluent.

Uranium Stripping Test Results Uranium was removed from the purified organic stream in stripping tests with water. The same pilot-plant equipment was used in the stripping tests as had been used in the TBP acidification and uranium purification (scrubbing) tests. For the stripping tests, purified TBP-HNO3-Uranium solution from the scrubbing tests was re-dissolved in SC CO2 and pumped upward through the packed column as deionized water was pumped downward through the column. The uranium content was measured in the organic and aqueous phases at the conclusion of each test to determine uranium stripping efficiency. Uranium stripping efficiency is a function of the nitric acid concentration of the organic feed, the organic-to-aqueous flow ratio, and the column height. In general higher aqueous flows improved uranium stripping. As would be expected, the uranium stripped more readily under low-acid conditions, from either increasing the water flow or with a lower acid content in the organic. The water addition rate, however, is limited by the potential for column flooding and by the need to avoid excessive dilution of the uranyl nitrate which is to be recycled into the AREVA chemical conversion process.

Intermediate-Scale Tests In 2008, AREVA installed an intermediate-scale separations column to help scale up the SC CO2 uranium recovery process. AREVA determined that data from the small, one-inch columns was not sufficient to provide the design basis for the full-scale process and that tests at an intermediate scale were necessary to reduce scale-up risks. The objectives of the intermediate-scale tests were to determine acceptable column configurations, including height and diameter, and optimize process parameters for the separations columns planned for the full-scale plant.

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Figure 7. Small (0.8 m) Scrub/Strip Column Test Apparatus The intermediate-scale column test equipment comprised an 18-foot (5.5 m) tall, three-inch (0.77 m) ID column (Figure 8) and supporting pumps, tanks, and instrumentation. The column was fabricated in three, six-foot-long (1.8 m) sections so that aqueous strip and scrub solutions (water and nitric acid) could be fed into the column at the top and at each junction. The column was wrapped in a copper water-heating coil and insulated to maintain a constant temperature. All feed streams, liquid CO2, TBP, water, and HNO3 were preheated in a tube-in-pipe heat exchanger. Because of the larger inventory of process solutions and CO2 the column and supporing equipment skid were placed inside enclosures to contain any CO2 leaks. For each test TBP feed material generated in extraction tests in the small pilot plant was mixed with SC CO2, heated, and fed to the bottom of the column. Acid or water was pumped to the column from the skid to remove impurities or strip out uranium. The TBP-SC CO2 mixture exited the top of the column and was sent back to the skid where it was depressurized and sent to the TBP-CO2 separator. The TBP from the separator was collected and analyzed and the gaseous CO2 was condensed and recycled. 74 In Nuclear Energy and the Environment; Wai, C., et al.; ACS Symposium Series; American Chemical Society: Washington, DC, 2010.

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Figure 8. Intermediate-Scale Column Key Intermediate-Scale Test Results Flow tests conducted with various packing materials demonstrated the operating flow rates achievable before flooding (aqueous carryover with SC CO2-TBP) occurred. The tests were made using SC CO2 and TBP near the expected operating pressure and temperature with water introduced at the top of the column. Tests at the maximum flow capacity of the pilot plant CO2 and TBP feed pumps with the smallest-size packing produced a small amount of aqueous carryover (about 1 percent of the total water input), no carryover occurred when the water to CO2-TBP ratio was reduced sufficiently. The column was more susceptible to flooding with smaller packing, but there was a trade off. 75 In Nuclear Energy and the Environment; Wai, C., et al.; ACS Symposium Series; American Chemical Society: Washington, DC, 2010.

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Smaller-size packing also provided a larger surface area, and therefore, better mass transfer. The intermediate-scale experiments tested various configurations for uranium purification (scrubbing). The best configuration for impurities decontamination other than gadolinium - was with the top third of the column used for water scrub and the bottom two thirds of the column used for nitric acid scrub. Gadolinium decontamination, however, was better with the top two thirds of the column used for water decontamination. This implies that there will be a trade-off between decontamination factors for different contaminants when setting parameters in the large-scale system. The nitric acid concentration in the scrub stream was the second-most important process parameter for scrubbing, with high nitric acid producing the best decontamination. Uranium was removed in stripping tests from the SC CO2-TBP mixture as uranyl nitrate by a counter-current downward flow of water. The column configuration, packing size, and acid concentration had an impact on uranium removal. As expected the taller column removed more uranium and smaller-diameter packing performed better than larger packing. This was due to better mass transfer from the higher specific surface area of the smaller packing. Uranium stripping was better for lower nitric acid concentrations.

Full-Scale Process Implementation AREVA completed construction of its full-scale industrial ash uranium recovery process in late 2009. The facility is designed to implement a clean and cost-effective SC CO2 uranium recovery process with the capacity to treat AREVA’s ash and that of potential customers. The facility is to be operated under AREVA’s Nuclear Regulatory Commission (NRC) special nuclear materials license and, as such, must meet NRC requirements for nuclear and industrial safety. Prior to beginning installation, AREVA conducted an integrated safety analysis in which the impact of process design and expected operating parameters on nuclear, industrial, and chemical safety was analyzed. AREVA’s integrated safety analysis had a significant impact on the final design of the process, especially in the areas of improved material handling, chemical and ergonomic safety, and nuclear criticality safety. The SC CO2 uranium-recovery process is installed in an existing uranium chemical conversion building on the Richland, Washington site and covers approximately 1100 square feet of a high-bay room. The process utilizes much of the building’s existing infrastructure, including utilities and intermediate storage tanks. Because of the potential for personnel exposure to uranium and harmful chemicals, the process equipment is installed in a ventilated enclosure. Most process operations are automated and manual operations are conducted through glove ports. The process comprises four main operations, 1) ash pail in feed and extractor basket loading, 2) uranium extraction, 3), uranium purification and 4) spent-ash handling. Incinerator ash is supplied to the system in pails of approximately five-gallon capacity. The ash-storage pails move from the in-feed bucket queue into a 76 In Nuclear Energy and the Environment; Wai, C., et al.; ACS Symposium Series; American Chemical Society: Washington, DC, 2010.

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containment hood for processing. The containment hood encloses the ash processing equipment that includes a crusher, a tumbler/mixer, and the extraction basket loading station. Ash clinkers may be present, so the contents of each pail are sifted and clinkers are routed through a crusher for size reduction. The ash and processed clinkers are then blended together and transferred into an extraction basket. The basket is then placed into an extraction vessel for uranium extraction. The extraction module is shown in Figure 9 being unloaded at the facility. An overhead crane is used to move the baskets in and out of the extractors. The extractor vessels are designed to preclude accidental opening under pressure. The uranium purification module comprises the counter-current packed columns, feed tanks and pumps, and a heat exchanger to preheat streams fed to the columns. Each countercurrent column contains a packing material that facilitates mass transfer between the SC CO2-TBP and aqueous liquid phases. Personnel exposure to CO2 or aerosols from a release of the working fluid is precluded by primary and secondary containment that have management measures in place to ensure that they are available and reliable when needed. At the completion of an extraction cycle an operator removes the spent ash basket from the extractor vessel using an overhead crane and places it in the uranium assay station. Two separate uranium assays are performed before the basket is allowed to move from the assay station to the emptying station. The spent ash residue is packaged in drums suitable for disposal at a licensed nuclear waste disposal site. The spent-ash handling operation is also enclosed in a ventilated glove box to protect the operator from contact with hazardous dust.

Figure 9. Extraction Module Delivery 77 In Nuclear Energy and the Environment; Wai, C., et al.; ACS Symposium Series; American Chemical Society: Washington, DC, 2010.

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Conclusions AREVA, in cooperation with University of Idaho, spent six years in developing and implementing an innovative new process for uranium recovery from incinerator ash and other low-uranium-content materials based on supercritical CO2 technology. Implementation of the technology required several stages of bench-scale and pilot-plant development. AREVA and University of Washington engineers and scientists designed and operated bench-scale and pilot-plant scale equipment at AREVA’s Richland, Washington fuel fabrication facility that developed the chemistry, process, and equipment necessary to implement a commercial-scale process. In 2009, AREVA finished construction of a full-size, industrial ash-uranium recovery facility at its Richland, Washington plant that will be operational in 2010. The new ash uranium-recovery process is important to AREVA because it allows economic recovery of enriched uranium from incinerator ash using a safe, environmentally friendly technology.

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